The Guys Take Daytonastein and the IROC to the
Track
September 22nd, 2004
The Event:
It was a pleasant Wednesday morning. Mike and Ed had both
escaped from the
salt mines for a little mid-week engine roaring, tire roasting
excitement. Both were eager to get to the track. The venue
was Muncie Dragway and
they were going to a private event. One of Mike's long time
buddies and his coworkers from GE in Ft. Wayne had rented out the track
from 10 - 3. This was what they were calling "Drag Day II", the
second time they rented out the track. There were 52 people on
the guest list although it didn't feel like there were near that many
in attendance. 10:00 - 1:30 was open racing... just get in
line. 1:30 - 3:00 was bracket racing.
Mike rose early and met Ed at his place just before 8am. By the
time he got there, Ed had Daytonastein loaded onto the tow dolly and
the Voyager was set to start another long haul. They caravanned
to
the strip, a little over an hour away, unloaded, and then contemplated
what to do next. Once the safety meeting was over, the fun
began. Looking around at the cars of the other participants, it
was clear that Mopars were not common at this event. With the
exception of
Daytonastein and Mike's IROC, there was one old school Mopar and a
fairly new looking Dodge Dakota. Aside from that, it was a slew
of Camaros, Mustangs, and Corvettes along with a couple BMWs, a couple
motorcycles, and a few other miscellaneous vehicles. The most
unexpected vehicle was probably the Honda Civic Hybrid which was the
only Honda and the only Hybrid in attendance.
The Cars:
Daytonastein - Daytonastein to date
had not been tested, had not yet gotten an
alignment, and really had not been driven for any distance worth
speaking of since the early blowing of a halfshaft. With the
exception of the turbo setup itself (and the wide array of parts from
which the car is built) the car has zero performance mods.
Restrictive tail pipe & muffler from the old 2.5, unported plenum,
standard 46mm TB, etc. etc. etc. Thus, no one really knew what to
expect. The wastegate
had been set to open as low as it would go, and this was being viewed
as a good day
to do some tuning. The fuel supply was composed of a simple set
of 26# injectors and a single cold start injector on a pressure switch,
again set to fire at low pressure. The A/F would be monitored via
a DMM and the runs recorded using Ed's scan tool.
While waiting around, a number of people took a look under the hood of
Daytonastein. It seemed that the conglomeration of brightly
colored yellow hoses, mismatched spark plug wires, and shiny brass
fittings caught the eye of the unsuspecting and solicited a quick,
"WTF?!?" One guy in particular took a lot of interest and chatted
with the guys awhile about the setup. It's probably safe to say
that everyone else's mods came from nice expensive aftermarket kits and
that Mike and Ed were the only "mad scientists" there. ...but
here at Kelly Mulhern Performance, we wear the DIY, home brewed, mad
scientist persona like a badge of honor. That is after all, what
we're all about. A Little Insanity + Some Confidence + Some
Experimentation = Innovation.
IROC - The IROC had just recently received a new
experimental set of ported heads from Ed back over Labor Day
weekend. During that point and the next few weeks, Mike was sick
and didn't have much energy to work on the car. Reassembly after
the addition of the heads encountered a number of unrelated problems so
Mike didn't actually get the car running properly until the night of
Monday the 20th ...2 days before the event. The car didn't
even leave his driveway until Tuesday and then perhaps 10 miles were
put on the car locally. In the week preceding the event, it
because increasingly unlikely that the IROC was going to be in
attendance, meaning that Mike would have been driving EJ's (Ed's 5yr
old son's) race car - '87 Shadow 2.5L, intercooled, turbo, A520
5-sp. In the end though, with the car finally running and
not many miles on the new heads, Mike said, "ah.. what the hell" and
decided to go for it.
On the way to Ed's, a 3hr drive, Mike gained some confidence by not
hearing any bad noises but thought that the car felt a little
sluggish. Regardless, he stopped on the rural road right before
Ed's and practiced a few burn outs while keeping an eye on the A/F
ratio to see what it would do. A later check of the timing at the
track revealed that it was set at about 5 degrees... as opposed to the
stock 12. Mike and Ed quickly advanced it to 15 (Mike filled up
with premium in anticipation of this) and the car seemed a bit
happier. So at that point, the IROC was set up with all the
"typical" mods, the ported heads, and the header prototype.
The Runs:
Daytonastein - Ed and Mike got in 4 runs with
Daytonastein. Why both? Ed did the driving. Mike
monitored the A/F ratio and the boost calling it out to Ed as he
watched the track. Unsure of what to expect, the guaranteed the
guys would know exactly what was going on and react as quickly as
possible in the event of leaning out or over boosting. The goal
was simply to keep it pig rich, run 4-5 psi of boost, and gently test
the car listening for anything that didn't sound good.
"Gently"... yeah right.
On the very first run, Daytonastein showed that it was full of
surprises. Ed hammered the gas and Mike monitored the A/F while
trying to find something to hold onto. In that first run, the
guys discovered that Daytonastein has some mighty fierce torque
steer. Upon launch, the car started shaking... washers, spare
parts, etc... rattled and rolled off the dash and the car lept
forward. Ed then slammed the car into second and the car swerved
under the toque steer with Ed pulling it back straight in white
knuckled excitement. The A/F ratio wasn't looking good so Ed
lifted up on the gas a few times. Interestingly, by the end of
the run, the O2 sensor seemed to wake up. Mike was seeing some
0.85s in the first pass and which didn't seem to make much sense
because the number wasn't moving during the shifts. Prior to the
run, it seemed stuck at .40 and then .50. At the end of
the run, the car seemed to rediscover closed loop and the oscillation
made the guys decide to try again now that the O2 sensor was
warm. It's likely that the first run went off before the O2
sensor had even fully warmed up and started telling us anything useful.
The second run confirmed the O2 sensor theory. During it Mike
observed A/F ratios in the 0.92 to 0.96 range. Falling out of WOT
during shifts, the numbers dipped as expected. Ed still lifted a
few times, listening to the car, fighting the torque steer, and trying
to get a feel for things.
During the third run, Ed and Mike realized that in their excitement,
neither of them had been really watching the boost. Ed caught
site of it during pass two and saw something between 5 and 7psi at one
point. Mike agreed to watch the boost on this run and then
promptly forgot as they raced down the track. Ed managed to
confirm 8psi during one glance down. Mike watched as the A/F held
at a rock solid 0.96. Ed let off early while the guys discussed
their next pass.
For the forth pass, Mike held the DMM up to the boost gauge so that he
could see both at the same time. Ed set up the scan tool to
record the run. While watching the boost gauge, Mike looked on in
mild shock. Daytonastein hit the 5-7 range all right. It's
also passed 8. In fact, at the height of one pass, it went all
the way to 12.5psi!!! The A/F ratio never even blinked. It
climbed to 0.96 after the shifts and held steady. Again, Ed
lifted, but both were impressed and perplexed by the high boost, the
A/F ratio, and the fact that what they were seeing didn't really make
much sense with the setup.
Spectators of the 4th pass apparently got a spectacular show as one of
the coolant lines began leaking and created a massive steam cloud
behind the car. In their intense contemplation, the guys didn't
really notice this, but one onlooker assured them that that had blown
the engine
and had no oil left in the crankcase. Later inspection revealed
that there was a small oil leak but that there was plenty of oil...
The coolant itself was a little low (maybe a cup), but not anything to
get excited about. A review of the recorded run proved that
the A/F ratio had actually held at 0.96. Lots of head scratch
then ensued.
IROC - Mike got in 5 passes on the IROC before bad things
happened. Prior to this event, Mike had never been to any track
in any car and had actually not even ever been a spectator at a
track. So really, he had no idea what to expect nor had he
practiced launches based on the light tree or anything else.
Run #1 was pretty much an excercise in panic. Mike's thoughts
& actions went something like the following:
"Am I in position. A little more.... a little
more. Sh$t I rolled too far foward! Gotta back up."
*Turns off car* *Puts car in Reverse* *Starts
car & backs up* *puts car in first* *pulls back forward*
(can't put it in reverse with engine running)
"Ok now I'm there. Wonder when I should gun
it? Ahhh!!! the lights are going down... I'm not ready. Go
go go!!!"
*rattle rattle rattle* "Holy Sh$t this is rough!"
"Where did the other guy go?"
"Ok, I'm a redline... shift!!!" *screech*
"Whew... now I got it."
Run #2 was a little better, now knowing what to expect, but it wasn't
good either. Mike dumped the clutch too quickly and it
held. The IROC's rpms plummeted to 1500 and the car rolled
forward as if driven by someone's cautious grandmother.
Run #3 was a great launch, at least compared to #1 & #2 but the
trans wouldn't go into 3rd. GRIND!!!! They synchro had been
going out and he had been getting some grind into 3rd with regular
driving so this wasn't terribly surprising. Mike remembers noting
that he was actually ahead of the other car during the first instant of
the launch which kind of made his morning.
Run #4 also had its problems. Most likely, Mike caught some water
from the water box while trying to go around it or someone else dragged
water out to the starting line. Mike gunned it, let out the
clutch, and then realized he was sitting still at 5000 rpms approaching
the 2nd gear shift and not moving. Based on how sticky the track
was in previous launches, water seems to be the only reasonable answer.
Run #5 was the fateful run, ending Mike & Ed's day at the track and
killing the IROC's a543. In this run, Ed was riding shotgun to
keep an eye on the IROC's A/F ratio, mostly out of curiosity.
The launch was nothing to really talk about although at the time, Mike
thought it was a great. Excited, he slammed the car into second
as he approached the redline squealing the tires and continuing the
run. Then at redline again, Mike missed his shift into 3rd and
instead slammed the trans into 1st. Rapidly decelerating, engine
screaming, Mike managed to get the car back out of 1st and into 2nd,
but the damage was already done and the trans was not happy about
shifting. Upon further testing in the parking lot, Mike found
that it was pretty much impossible to shift into or out of any gear
with the car running (lots of force, no grinding, no result) and that
shifting could only be done with the motor off.
For those interested, Mike's times were as follows:
| Run |
1 |
2 |
3 |
4 |
5 |
| R/T |
1.212 |
1.076 |
0.749 |
1.049 |
1.094 |
| 60 |
2.627 |
2.764 |
2.402 |
2.930 |
2.419 |
| 330 |
7.049 |
7.218 |
6.738 |
8.180 |
6.797 |
| 1/8 |
10.659 |
10.809 |
10.622 |
11.950 |
11.396 |
| MPH |
68.450 |
68.980 |
61.670 |
65.720 |
47.590 |
| 1000 |
13.725 |
13.863 |
13.922 |
15.105 |
16.497 |
| 1/4 |
16.281 |
16.416 |
16.660 |
17.700 |
21.527 |
| MPH |
89.480 |
89.500 |
79.820 |
88.490 |
43.260 |
Final Thoughts:
Daytonastein - After Daytonastein's debut, KMP has now
officially renamed the "quarter
mile" the "2/7ths mile" due to the torque steer induced, slalom like
runs. The runs themselves, didn't produce very interesting times
because Ed frequently let off the gas to be safe and was
continually fighting torque steer. The times themselves though
were not point of this adventure so the guys were pretty happy.
Despite being unaligned, not even pushing WOT through the entire run,
Daytonastein still managed a 15.9@ 73mph with driver, one passenger and
a full interior (including spare tire). Not bad for first outing.
Upon further review of the car, it was discovered that one of the
vacuum hoses had blown off of the detlagate which allowed the boost to
rise more or less uncontrolled. This explains how 12.5 psi could
have been achieved.
Current speculation is that the restrictive stock 2.5L exhaust pipe and
muffler created a large amount of back pressure effectively plugging up
the exhaust and preventing the real power of the 12.5 psi of boost from
being unleashed. Some initial fuel calculations show that
Daytonastein should only have enough fuel for about 8 psi so this could
explain how the ratio held at 0.96.
Hopefully after an alignment, opening up the exhaust, and getting a
little more practice with the car, it will perform much better.
IROC - Mike wasn't too upset by the loss of the transmission
and is excited to try again once he replaces it. Fortunately, a
spare is currently sitting in his garage awaiting installation.
With a cleaner shifting trans and a little more practice, his times
should come down. Once the new transmission is installed, Mike
will do some testing to see what the impact of the ported heads
is. Assuming all goes well some significant mods are planned for
later this winter and next spring.
3.0 Toughness - Mike's first assault against the 3 Liter
happened in the IROC when he managed to engage the transmission in 1st
from 2nd gear redline. The result is that the motor would have
spun beyond 7000 rpms, over 1000 rpms beyond redline. Despite
this unfortunate event, the motor held and continues to sound just
fine.
Mike's day of torture testing 3 Liter engines wasn't over with over
reving the IROC's engine! With the IROC being towed home, Mike
got to drive Daytonastein back to Ed's place. At some point
during the hour drive the coolant line to the turbo blew off. The
guys didn't discover it until well after they got to Ed's and the car
had cooled down. Ed reconnected the line and filled the car with
coolant the following day. Daytonastein started up and drove like
normal... No problems!
That said, Mike has now established that a stock Chrysler 3 Liter is a
STOUT engine! It can handle over 7K RPM and cruising for an
extended time with _no_ coolant! Don't try this at home folks,
Mike is a trained professional! And never try it with a Ford or
Chevy! :)
Ed & Mike at the track:
